Spoiler alert: NEVER mix wine, heat and Hammond plastics….. else, read on…
There have been many posts and advices given in regards to how to do both full-foldback and manual tapering for Spinet series organs (in my case a M100). I am sure that there are many that have been very successful in performing these modifications, and I am sure that there have been a number of stories where a job has gone horribly wrong resulting in a ruined manual.
I ordered an upper manual foldback kit off Ebay (Alan Dubois) just before Xmas with the intention of making the installation a nice little project between Xmas and New Year. The kit arrived as a well presented set of key contacts with clearly written instructions.
I was pleased to be able to make a start. The first thing that I did was create a new spreadsheet that clearly represented the works I was to do from the visual perspective that I would be working.
FOLDBACK
I set about the foldback activity first and found that inserting the new contacts was a relatively simple, if not Zen like activity to do. There was a certain ‘pleasure’ when one felt the new contact just ‘clicking’ into place without having to fiddle with a pick in order to get it through the correct guide hole. I approached the job based upon frequency order and when completed, soldered the ends off at the appropriate frequency lug.
First set of contacts installed, frequency 80, lots to go…
TAPERING
After inserting the 48 new key contacts for the foldback job, I then set about the tapering activity. This involves soldering 36 x 27 Ohm resistors in parallel with the existing 16 Ohm resistor wires to obtain the desired 10 Ohm resistance. Again, a job that I worked carefully and methodically through and found quite enjoyable as it was similarly Zen in nature.
After tidy up, I thought to myself that I had done a very neat/tidy job and deserved a glass of wine or two to celebrate my apparent success. See below:
Foldback and tapering complete... and with a nice tidy wiring loom
All in all, looking like a damn fine job.
Whilst having a well deserved glass of red, I thought that I might return to my work and just use a mini heat gun with a small nozzle to ‘tighten up’ the heat shrink and make an already tidy job into a ‘piece de resistance’. Thus, I very carefully applied some hot air to the heat shrink keeping in mind that I am working near plastics and was thus very careful to keep the nozzle pointing upwards. I then retired for the evening feeling very pleased with myself.
BAD MOVE
When I came to check continuity, I found that some of the key contacts had frequencies that spanned several frequency lugs. Knowing that this is definitely not correct, I took a careful look and discovered ‘horror of horrors’ that my upper contact support plastic had warped (due to the heat). I had one of those gut wrenching epiphanies that again told me never to mix heat (wine) and plastics!!
Oh dear, warped chassis plastics resulted in numerous key-contacts being in contact with the busbars.
I never thought to look at the actuators that had lifted because I assumed that they were pulled upwards due to the warping.
SOLUTION
If I were to be living in the US, then the solution would most likely have been to simply grab another upper manual from some ‘donor’ M100 (given that they still seem to be plentiful). However, I live in Australia and the story is much different. Hammonds and Leslies (and parts) are becoming scarcer than ‘hen’s teeth’ so it was once again off to the US to purchase some replacement chassis parts. This I managed to do and one week later they arrived.
THE FIX
I determined that I would need to be very careful in managing the key-contacts and resistance wires as I removed them. Previous experiences with the enameled wires told me that they can very quickly become a terminally tangled rats-nest. I resolved to use an additional piece of chassis plastic to act as the temporary storage bin of the individual contacts as I removed them from the damaged chassis. This scheme worked out very well and also provided the benefit of not having to label every key-contact removed.
Removing the key-contacts and storing to the temporary storage assembly
The forum only allows 5 attachments/images per post so please read on in Part 2..
There have been many posts and advices given in regards to how to do both full-foldback and manual tapering for Spinet series organs (in my case a M100). I am sure that there are many that have been very successful in performing these modifications, and I am sure that there have been a number of stories where a job has gone horribly wrong resulting in a ruined manual.
I ordered an upper manual foldback kit off Ebay (Alan Dubois) just before Xmas with the intention of making the installation a nice little project between Xmas and New Year. The kit arrived as a well presented set of key contacts with clearly written instructions.
I was pleased to be able to make a start. The first thing that I did was create a new spreadsheet that clearly represented the works I was to do from the visual perspective that I would be working.
FOLDBACK
I set about the foldback activity first and found that inserting the new contacts was a relatively simple, if not Zen like activity to do. There was a certain ‘pleasure’ when one felt the new contact just ‘clicking’ into place without having to fiddle with a pick in order to get it through the correct guide hole. I approached the job based upon frequency order and when completed, soldered the ends off at the appropriate frequency lug.
First set of contacts installed, frequency 80, lots to go…
TAPERING
After inserting the 48 new key contacts for the foldback job, I then set about the tapering activity. This involves soldering 36 x 27 Ohm resistors in parallel with the existing 16 Ohm resistor wires to obtain the desired 10 Ohm resistance. Again, a job that I worked carefully and methodically through and found quite enjoyable as it was similarly Zen in nature.
After tidy up, I thought to myself that I had done a very neat/tidy job and deserved a glass of wine or two to celebrate my apparent success. See below:
Foldback and tapering complete... and with a nice tidy wiring loom
All in all, looking like a damn fine job.
Whilst having a well deserved glass of red, I thought that I might return to my work and just use a mini heat gun with a small nozzle to ‘tighten up’ the heat shrink and make an already tidy job into a ‘piece de resistance’. Thus, I very carefully applied some hot air to the heat shrink keeping in mind that I am working near plastics and was thus very careful to keep the nozzle pointing upwards. I then retired for the evening feeling very pleased with myself.
BAD MOVE
When I came to check continuity, I found that some of the key contacts had frequencies that spanned several frequency lugs. Knowing that this is definitely not correct, I took a careful look and discovered ‘horror of horrors’ that my upper contact support plastic had warped (due to the heat). I had one of those gut wrenching epiphanies that again told me never to mix heat (wine) and plastics!!
Oh dear, warped chassis plastics resulted in numerous key-contacts being in contact with the busbars.
I never thought to look at the actuators that had lifted because I assumed that they were pulled upwards due to the warping.
SOLUTION
If I were to be living in the US, then the solution would most likely have been to simply grab another upper manual from some ‘donor’ M100 (given that they still seem to be plentiful). However, I live in Australia and the story is much different. Hammonds and Leslies (and parts) are becoming scarcer than ‘hen’s teeth’ so it was once again off to the US to purchase some replacement chassis parts. This I managed to do and one week later they arrived.
THE FIX
I determined that I would need to be very careful in managing the key-contacts and resistance wires as I removed them. Previous experiences with the enameled wires told me that they can very quickly become a terminally tangled rats-nest. I resolved to use an additional piece of chassis plastic to act as the temporary storage bin of the individual contacts as I removed them from the damaged chassis. This scheme worked out very well and also provided the benefit of not having to label every key-contact removed.
Removing the key-contacts and storing to the temporary storage assembly
The forum only allows 5 attachments/images per post so please read on in Part 2..
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