Yesterday, I paid a visit to a church that had a Hammond BC, which had a non-functioning chorus generator. I was very disappointed to discover it was not a simple motor problem, but a drive shaft problem. I had hoped it was a "relatively" straight forward issue of a broken or missing brass paddle linkage. However, upon removing the chorus generator and inspecting it on the bench, I found the problem was not at all the paddle. All paddles were accounted for. The problem was that the brass gear was loose on its shaft, and not engaging the shaft. These gears are pressed on to the shaft at the factory, so you might call this a "bad pressing", but I'm not a machinist, so don't quote me on the diagnosis. All I know is that the gear was spinning freely on its shaft.
It looked like a blob of solder was stuck near the gear on the shaft, which was evidence that in the past, someone had repaired this thing with solder. As to whether their repair was a success or not, I can't say. This chorus generator has never worked in the time the organ was owned by this person, and no one had heard any difference.
Any sane person would have found a donor chorus generator, but I skirt the boundaries of sane sometimes, and the reason I did it was, I thought about the ways to fix this.
1. Replace the entire chorus generator.
2. Find a donor shaft segment (each segment has 4 gears on it), do major surgery to replace that shaft segment. (Does not make sense unless somebody happened to have disassembled (partly or completely) a donor chorus generator. The gear ratios are unique to this type of generator.)
3. Remove the faulty shaft, and have it welded, or braised. My knowledge of this topic is non-existent, but someone suggested braising, and I thought, forget it, because I can't do anything involving great amounts of heat so close to the phenolic clutch. It would melt or warp the phenolic. I'd have to remove the shaft first.
4. My father suggested cold solder. I don't know what he is referring to. (Anyone want to chime in?) I know what a cold solder joint is, and it's not a good thing.
5. Some other type of glue (epoxy).
After discussing the options at length with the owner, we agreed to give epoxy a shot. I used JB Weld 4400 strength 5 minute set 1 hour cure time epoxy. I cleaned the area repeatedly with CRC QD cleaner, and denatured alcohol. I then rubbed the shaft and gear with some 220 grit sandpaper (not easy to do, had to use forceps to reach in and do this.) Once I was satisfied everything was burnished and clean, then I mixed the epoxy and applied it with a thick syringe on the area. I had to be careful to watch for drips, because any epoxy that got on the gear teeth would ruin the gear. I did this on both sides of the gear. I waited about 30 minutes, gently rotated the shaft and did the same thing to the other "half" of the gear. I gave it more than a full hour to cure. I slowly turned the shaft by hand and it engaged. Finally, I applied power to the start motor, and it started up successfully. To stress test the repair, I hit start on the bench several times in succession just to see if it would compromise the joint in any way, and it did not.
I reinstalled the generator, and it is running beautifully. Because this was a repair I have never done before, and because the longevity of the fix is not known, I am being very generous with warrantying my work here for a long period of time, should this fail in the future.
This is only the second chorus generator I have ever heard working in person, and it happens to be only because I repaired it. That is very satisfying, to say the least.
I'll post photos later, just wanted to share the experience with you all while it was fresh on my mind.
It looked like a blob of solder was stuck near the gear on the shaft, which was evidence that in the past, someone had repaired this thing with solder. As to whether their repair was a success or not, I can't say. This chorus generator has never worked in the time the organ was owned by this person, and no one had heard any difference.
Any sane person would have found a donor chorus generator, but I skirt the boundaries of sane sometimes, and the reason I did it was, I thought about the ways to fix this.
1. Replace the entire chorus generator.
2. Find a donor shaft segment (each segment has 4 gears on it), do major surgery to replace that shaft segment. (Does not make sense unless somebody happened to have disassembled (partly or completely) a donor chorus generator. The gear ratios are unique to this type of generator.)
3. Remove the faulty shaft, and have it welded, or braised. My knowledge of this topic is non-existent, but someone suggested braising, and I thought, forget it, because I can't do anything involving great amounts of heat so close to the phenolic clutch. It would melt or warp the phenolic. I'd have to remove the shaft first.
4. My father suggested cold solder. I don't know what he is referring to. (Anyone want to chime in?) I know what a cold solder joint is, and it's not a good thing.
5. Some other type of glue (epoxy).
After discussing the options at length with the owner, we agreed to give epoxy a shot. I used JB Weld 4400 strength 5 minute set 1 hour cure time epoxy. I cleaned the area repeatedly with CRC QD cleaner, and denatured alcohol. I then rubbed the shaft and gear with some 220 grit sandpaper (not easy to do, had to use forceps to reach in and do this.) Once I was satisfied everything was burnished and clean, then I mixed the epoxy and applied it with a thick syringe on the area. I had to be careful to watch for drips, because any epoxy that got on the gear teeth would ruin the gear. I did this on both sides of the gear. I waited about 30 minutes, gently rotated the shaft and did the same thing to the other "half" of the gear. I gave it more than a full hour to cure. I slowly turned the shaft by hand and it engaged. Finally, I applied power to the start motor, and it started up successfully. To stress test the repair, I hit start on the bench several times in succession just to see if it would compromise the joint in any way, and it did not.
I reinstalled the generator, and it is running beautifully. Because this was a repair I have never done before, and because the longevity of the fix is not known, I am being very generous with warrantying my work here for a long period of time, should this fail in the future.
This is only the second chorus generator I have ever heard working in person, and it happens to be only because I repaired it. That is very satisfying, to say the least.
I'll post photos later, just wanted to share the experience with you all while it was fresh on my mind.
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