I’m trying to determine if there is something I did that caused the electrolytic can to fry. Before I launch into my blown can question, I’ll set it up with the order of events.
I recently purchased a Tallboy that had all of the components but not wired up (speakers, motors, etc…not plugged into the amp). Previous owner had work done on the amp (a few caps from what I can see) and never got around to finishing the project. All caps measured fine, 30/30/10 can all within 20% tolerance. This can not recently replaced as some other components - perhaps original.
I put the amp on the bench for the standard blow it out and inspect routine. I wired up AC to pins 3 and 4, and an audio input (phone thru a headphone amp) to pins 1 and 2, a 16 ohm speaker (not the field coil) and fired it up. To my relief, the amp worked and only had minor hum (which I attributed potentially to my input rig).
2 Speed conversion: I removed the source A/C (orange wire - pin 4) from the “always on” outlet. The outlet was used to bus the fuse, the relay source, and the 0.1 uF cap from the switched outlets….so I removed all from the outlet and used a wire nut for now. The outlet at this point is open with only common still wired to pin 3. I ran the source side of the outlet to the brake socket pin 4 - a bus point for the (NO) side of the relay switch. I double checked by eye and also used a continuity meter to verify the wiring - manually pressing the relay to simulate switching. I made no other alterations other than cleaning up the relay contacts.
Some days pass and the next step was to test the crossover and drivers. AC and input wired as above, I tuned it on and heard a loud hum and no audio. I removed the crossover and drivers, and wired the first speaker with the same results. The volume knob did not affect the hum level.
Next step was to yank power tubes one-by one. I found that one 5881 socket seemed to be the culprit and noticed that while making sure it was seated and pushing gently, all noise stopped - then when I let go it would hum loudly again. I found you can do this for no more than 6 seconds, because at 7 seconds the filter can pops and smokes (just in case you want to try this at home). From underneath, the socket was found to be loose in the chassis but otherwise appeared intact.
So can we first confirm that my 2-speed conversion is correct before we move on to the smoking can question? Then if we’re relatively confident that the conversion is not directly responsible, can someone give me trouble shooting guidance or post a previous topic thread?
I recently purchased a Tallboy that had all of the components but not wired up (speakers, motors, etc…not plugged into the amp). Previous owner had work done on the amp (a few caps from what I can see) and never got around to finishing the project. All caps measured fine, 30/30/10 can all within 20% tolerance. This can not recently replaced as some other components - perhaps original.
I put the amp on the bench for the standard blow it out and inspect routine. I wired up AC to pins 3 and 4, and an audio input (phone thru a headphone amp) to pins 1 and 2, a 16 ohm speaker (not the field coil) and fired it up. To my relief, the amp worked and only had minor hum (which I attributed potentially to my input rig).
2 Speed conversion: I removed the source A/C (orange wire - pin 4) from the “always on” outlet. The outlet was used to bus the fuse, the relay source, and the 0.1 uF cap from the switched outlets….so I removed all from the outlet and used a wire nut for now. The outlet at this point is open with only common still wired to pin 3. I ran the source side of the outlet to the brake socket pin 4 - a bus point for the (NO) side of the relay switch. I double checked by eye and also used a continuity meter to verify the wiring - manually pressing the relay to simulate switching. I made no other alterations other than cleaning up the relay contacts.
Some days pass and the next step was to test the crossover and drivers. AC and input wired as above, I tuned it on and heard a loud hum and no audio. I removed the crossover and drivers, and wired the first speaker with the same results. The volume knob did not affect the hum level.
Next step was to yank power tubes one-by one. I found that one 5881 socket seemed to be the culprit and noticed that while making sure it was seated and pushing gently, all noise stopped - then when I let go it would hum loudly again. I found you can do this for no more than 6 seconds, because at 7 seconds the filter can pops and smokes (just in case you want to try this at home). From underneath, the socket was found to be loose in the chassis but otherwise appeared intact.
So can we first confirm that my 2-speed conversion is correct before we move on to the smoking can question? Then if we’re relatively confident that the conversion is not directly responsible, can someone give me trouble shooting guidance or post a previous topic thread?
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